1、 , , , , 20.5%, , ; ; ; ; ; (1971-) , , , ( ) , , E-mail:Wcrdc- Application of variable-frequency regulating speed technology in compressor at natural gas booster station of gas turbine power plant Abstract Specific to the problems like the high energy consumption of natural gas compressor and the l
2、ow efficiency in using throttling governing in gas turbine power plant, in this study, the working principle, the regulating process and the matters needing attention of variable-frequency regulating speed technology incompressor were expounded and analysis was made onits energy efficiency. The oper
3、ation practice showed thatthe shaft power of the compressor could reduce by 20. 5% after the variable-frequency regulating speed technology was applied in the compressor, which presented significant energy-saving efficiency. It can be used as the reference for the energy-saving transformation for si
4、milar power plants. Keyword gas turbine; booster station; compressor; variable-frequency regulating speed technology; energy saving; 0 9E , 2.52.8 MPa, 0.40.7 MPa, , 1 , , 2; , 52%, 9E , , , ( ) , , , , , , 9E , , 2015 4 , 1 , , ( ) , , , , Q1=Q0 (n1/n0) , n0 n1, N1=N0 (n1/n0) Q0 N0 n0 ;Q1 N1 n1 , ,
5、 , , 2-3 , , , , 1 1 , , , , 2 , 0.4 MPa0.7 MPa , ; , 4 , ITCC , ITCC , , , , , , EBZ35-4+4 , 4 , 4 , 8 : Qe 4062743678 m/h, Pe2 2.841 MPa, ne 13920 r/min, Ne 3735 k W : 0.4410.8 MPa , (8 ) , ; 0.81 MPa , (8 ) ; 11.6 MPa , ( 4 ) , , , 1 MPa, , 4 5 3 , , , 1 390 A, 4043 k W; 2 310 A, 3 214 k W, , 20.5%, 829 k W 4500 h , 373 , , , , , , , , , , 6-9 4 , , 2 1 20.5%, 1 . J. , 2009, 2 (8) :56-58. 2 . M. : , 2002. 3 . M. : , 1994. 4GB 50251-2003, S. 5 , , , . M. : , 2010. 6 , , , . J. , 2010, 26 (5) :18-20. 7 . J. , 2013, 29 (4) :57-59. 8 . M. : , 2004. 9 . J. , 2008, 15 (1) :24-29.